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Fitting a 12 volt conversion kit This article is going to show how I fitted a GMC 12 volt alternator conversion kit to my 6 volt 1943 1 ½ ton Chevy. It should only be used for information purposes and not as a replacement for any instructions you receive with any similar kit you may buy. Neither MVWF nor myself will be held responsible for any damage or injury if you do not follow the original manufactures instructions when fitting a kit for yourself. The
kit I am fitting is the GMC alternator conversion kit from Jolley
Engineering. Below is the kit
with all its included parts. First
of all I removed the old Dynamo and wiring.
The original adjuster arm is reused, so I left this in place. Next
I fitted the new alternator bracket in place of the old dynamo bracket. As
I removed the alternator from its bracket in order to fit it, I have now
refitted the alternator to its bracket. Next
I looped the new belt onto the crankshaft pulley, water pump pulley and the
alternator pulley. I also
fitted the supplied extension bracket for the adjuster arm, as the original
was too short to allow me to tension the belt.
At
this point I found the first differences between the GMC and Chevy engines
and alternator fittings. The
alternator was set about ¼” too far back on the supplied bracket, so the
belt didn’t run inline. To
solve this I tapped the bush on the rear of the alternator out and fitted
one of the supplied spacers at the front of the alternator after grinding it
down to size. The
other problem I came up against was in order to tension the belt correctly
the alternator had to be pulled a lot further away from the engine than the
adjuster brackets would allow. To
solve this I have manufactured a new bracket, which has a curved section to
allow it to run over the contour of the alternator and allow me adjust the
belt tension correctly. With
alternator now fitted to the engine, it was time to start on the electrical
side of the kit. I connected
the supplied main cable to the back of the alternator.
The wires were supplied with crimped ends already fitted, so I fitted
the two yellow connectors onto the two large terminals on the back of the
alternator. I
then fed the wires through the bulkhead and connected the two ring terminals
to negative side of the ammeter. This
is the side connected to the ignition switch, not the side that
attached to the starter switch. Next
I had to fit the warning light. This
is required, as without it the alternator will not turn on its charging
circuit when the engine is started. I
have chosen not to drill any holes in my dash to fit the light, but instead
I have made a bracket to fit onto the side of the steering column. I
connected the blue connector to the small terminal on the back of the
alternator and fed it through the bulkhead before reconnecting it to the
warning light. Then
I connected the ring terminal to the ignition side of the ignition switch. Not the battery side. That’s it kit fitted. I estimate that without all the extras I had to do in order to make the kit fit my engine, it should take a mechanically competent person less than an hour to fit. As
I now have a 12 volt charging system fitted there are few other things on
the truck that require changing in order for them to work properly.
First of all I had to fit a resistor between the fuel gauge and
sender. This reduces the
voltage flowing to the 6 volt sender unit.
I had to fit a new 12 volt ignition coil to the engine. Then all the light bulbs/units had to be changed for 12 volt
bulbs/units.
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©2007 MVWF